Or so I’ve heard. Yesterday I decided it was a good to remove the slimline roof A/C units from the derelict “Luxury Traveller” motor home I dragged home earlier this summer. (Ah, those heady, dream filled days…) That soon lead to the thought that since I was tearing into it, I might as well keep going, and so, 7 hours later, this was the result.
As it turns out, the thing was built both much worse than I thought motor home construction was done, and much better at the same time. I thought the thing was stick and staple framed, and simply cut through the body in what I though would be manageable chunks, leaving the roof intact to cut up once it was all down.
Great plan. But…
The “but” is that the framing (?) of the coach was very thin wall aluminum tubing, every 2 feet, around the windows, roof vents, down the center of the roof and at the tops of the walls/roof joint where were two stacked together. Sturdy, and yet flimsy, all at the same time. Between the framing is 2″ blue foam board, bonded to luan with a vinyl face on the inside, and luan bonded to very thin fiberglass sheeting (brand name, “Filon”) on the outside. A leaky roof had led to water running down the left front corner and right rear, to the point that the luan inside and out, was completely rotted away, along with a few scraps of lumber where it was evidently too difficult to cut and from aluminum for structure, and a colony of carpenter ants had turned about a third of the wall at the right rear to a giant ant farm. It was awful.
The Sawzall, with new demo blades, didn’t notice much difference in resistance to the very thin aluminum (I thought I was cutting through 2×2’s), and at the top, behind and above the driver seat, my roof cut and upward wall cuts didn’t quite meet.
I thought this would simply tear apart, not knowing it was really aluminum I was cutting though, and when I tugged on the pull strap with the GMC to pull down the house, the cab, still attached to the roof, came with it. The “welds” (if you want to call them that) on the aluminum tubing “studs” were so poor where they met the one laying down at the floor, that they simply popped off, and the cab pulled completely loose all the way to the front.
This complicates the rest of the destruction a bit in that now I have to work under the partially collapsed cab to remove the gauges and enough of the wiring loose in order to keep it operable (it still starts up and runs) so I can get it moved close to the shop (where the tools are) in order to pull the engine/trans and strip the rest of the stuff off it I can use. Like the “Onan” generator, air suspension, and leveling jack system.
So, that’s what happened yesterday. Today I’m going to try to cut up the big chunks of wall and roof so I can stack them up, and so they won’t kill the grass in the back yard, and get ready to attend the “Relix Riot” this weekend.
Stay tuned for more progress on the motor home demo, and on the (hopeful) sale of the yellow Riv today…